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adventureleather

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About adventureleather

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  • Leatherwork Specialty
    Bags and pouches
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    Bag Making
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  1. I have had both 5100 and 4800, now a 205. The 205 is similar to the 5100/441 and leaves less marks than I have seen. Go figure. Something I always do is on a grinding wheel, I curve the sides, and back of the presser feed then hand sand them. After that I polish with my knife compounds. These machines need to be tailored to your type of leather since out of the box they are just generic. I love Herz Bags and watch their videos, some machines look super old and customized. I also sand down the throat plate and feed dog if needed. Next you can look at the presser spring, if it is all the way up and still too tight you can snip off a few coils of the spring. Be sure to have a spare incase though. I did that on the 5100, but didn't need to on my 205. I would start with the feet since rounding off the edges won't make a pronounced hard edge in the mark, but more a depress that can be hammered out. Be sure to watch for the material slipping though you're stitch length will change. If you top tension is too tight that will also move the material as the foot walks on a low pressured presser foot. If you don't want to grind the original feet, I get feet off of eBay and customize those since they are cheaper to replace. Also don't forget if you raise the feed dog, you're adding pressure. You'll have to make a machine adjustment to the new height with the centre foot and that just more fiddling. Those are some things that have helped me with chrome tan and veg tan like buttero. Some chrome tan that marks easy had bad marks before with the harder edges of the foot not rounded.
  2. Thanks Al. Totally understand. I had no choice..needed a better motor than what mine came with haha. Great questions. The SH model has more circuitry to help with the heavier machine for the torque of turning a bigger flywheel. I think for heat if you use the slower RPM settings. I don't recall the HP rating on the SL vs SH. The motor is well built very solid metal. Ryan mentioned to me that some saddler makers still like the reducer for the torque ability because they are used to it. But the pulley on the 750 is super small and the motor goes to 50RPM. For me it is super slow and powerful enough for my uses, 2.3mm 2 layers mostly and it is sewing fine with glue. I haven't trie thicker material. In terms of speed, yes no speed reducer needed..its very slow without. I didn't get the needle positioner. I didn't want to spend more and I haven't missed having one to be honest. The motor slows down immediately so finding BDC or full up is fine and easy.
  3. I wanted to chime in real quick on the 750SH. I am in Canada and Ryan Neel had the motor to me in 3 days! WOW what an awesome motor. I am using it with a 205 style machine from Global. My machine was used and came with a Reliable style motor (grey plastic cover) and was not great. A speed reducer would have cost me the motor alone. The Kindyne is super slow, and will easily go through my 2 layers of 2.5mm chrome tan on a 27 needle. It is well built, of course time will tell how long it lasts. The best thing about the motor setup is it is very responsive. Pedle movement starts it slow and the ramp is nice. Once you let up it immediately stops or slows. Very easy to control. I didn't get the NPS because I didn't want to bother with the flywheel I have and with the speed control I don't miss it. I have had the typical brushless servo motor coming from just about every industrial brand (they all look same with the logo changed) and didn't like the feedback. If anyone is questioning the Kinedyne it is a huge value and can transform your machine performance. Showing the slow speed of the 750SH
  4. It seems I have fixed and solved my own problem so I wanted to update this post incase someone searches and has a similar issue. With the help of old posts I have added some solutions to solve my problems too. And with respects to the take up spring, thank you to Uwe and Wiz for old posts on that topic. It seemed like my machine was not liking the thread. With a bit of an ear for how a machine should sound it did sound off to me. The weaver timing device came in the mail and it was a bit help to get the timing perfect and repeatable. Along with Uwe's stitching video that helped me guage a good timed machine. Although with variances of course to mine. Timing - this one took some time and many efforts to find the right balance. I ultimately set the needle bar to the eye of the bottom needle just above the angle ridge on the deflector. I then set the timing device to this spot, went up to the next spot of the needle bar for the device, and adjusted the hook. I have gotten goo stitched here for 23 to 27 needles I use. Needle placement in the deflector and guard - I didn't know how to do this one but I took a guess. There are 2 locking collars on either end of the timing shaft. 2 bolts in each. Loosen both collars and the timing shaft has a few mm of play. With the plate and dog off, you can put your largest needle you'll us in, and get the perfect spacing here. Push the collar in while holding the defecltor piece and tighten. It's a bit fidly. Now with the collar closest to the needle tight, the other one needs to be pushed in against the inner wall (body of the machine side underneath) and tighten. This locks the shaft from moving side to side and holds the deflector in place. Here you'll want to make sure the needle and hook pass nicely, and the needle can't be pushed in to the right if the material moves, jamming the hook into the needle. I pushed on my needle and moved the flywheel to ensure nothing could crash, but still have fluid movement. Now the largest 27 needle can pass nicely helping make the stitch. I am using all 3 sizes, so it is possible to hit the smaller needle with the hook if it moves since the machine is now set for the 27, something to keep in mind while sewing. Those 2 adjustments helped make a nice stitch. But I was stabbing the thread on the way down. Check spring tension and placement - thanks to an old discussion on this with Wiz and Uwe giving some info, it occurred to me the rule of the check spring. To keep the thread tight around the hook, and also that the thread should not have any slack until the needle hits the material. My thread had plenty of slack on the way down. So I moved the check spring bar all the way down. There is also a small Allen bolt to the left of the the secondary tensioner, loosen this and you can turn the thread bar further back over the discs. This will take away slack as well if more is needed with the bar down. And finally some more tension on the spring, locking bolt located inside the head to the left info on Weaver's dvd videos. Walking feet - last thing after all these adjustments is to make sure your feet are in good movement. So I set my need to just enter the foot hole, loosen the two Allen bolts on the back of the head (Uwe's video helps here) push the feet down, tighten and check movement. You can check your height too when the outside foot as at its highest. Last thing was to dial in tension. I also don't wind my bobbins too tight to allow them to unravel easier. After all that I am getting some great results and the machine and hook even sound more happy by sound. I am no expert, just from my little experience so don't take every word as proper instruction. Hope this helps another novice diagnose their Adler 205 style machine if you have any issues like I did.
  5. Thanks Glenn. It is Vinymo #1 thread, bonded polyester. I believe it is closer to 277 in size.
  6. Thanks kgg, I have seen Uwe’s video over and over now haha. Keep trying to see if I missed something. I had had 441 clone and 1342 clone before but never a 205 clone. Even watch the Weaver ones too. I re timed tonight with needle bar adjustments, I think I have it in a good spot. I re-worked the tension and got some good results. I noticed the twist at some points still. I wonder if it is something with the winding, hook (comes out tight some times) or just getting the tension balance. How tight would you wind 277 thread on a bobbin? My hook is also missing the inner spring, I wonder if that has any place for making it even or just to help take out the bobbin. Thanks for the feedback.
  7. Hello! I am hoping to have some skilled eyes to look at my stitches on an Adler 205-370 style machine. I have these random twisted bottom stitches from time to time. Or sometimes after stitching perfect the twist will pull the knot out. I am not sure what can be causing this. I have retimed the machine many times looking for smooth movement with weaver timing device. Does this on both needles I have 24 and 25. Any ideas? Thanks for the help!
  8. Hello, For Sale is a LIKE NEW Techsew 4800 PRO Cylinder Arm Industrial Sewing Machine. Purchased directly from Techsew in Quebec. It is only 1.5 month old and basically brand new. If you are looking for a walking foot sewing machine this will be a great deal for you. This machine is amazing for leather, vinyl, canvas, jean, fabric and many other materials. Everything works perfectly and is brand new. It is the PRO version which comes with the roller edge guide, laser guide, speed reducer and aluminum flat bed attachment. I have a lot of accessories for it including left, right and double narrow presser feet and many needle sizes and types, and spare bobbins. This will be a complete package for anyone looking to get a cylinder arm machine. Size 210 thread is available for an extra price. The machine is not able to transport easily so viewing and testing will be in Uxbridge, Ontario, Canada. The whole package is $4700. With shipping it is $5400 from Techsew. Please contact me if you have any questions.
  9. Thanks Glenn I was thinking the same. Though I’m confused because Juki does list 138 to work. The shop was having issues with thinner thread too a so they’re trying to solve it. Thread is getting cut. Something is out I’m guessing.
  10. Thanks I’ll ask if needed. I did see chris once for some needles and foot and he was expensive. At the time I didn’t check and just grabbed them. Didn’t like that. Best to know what I’m getting next time before I pay.
  11. Thanks Kgg, yes I did see that. I have 138 vinymo only right now and the issue persists. Might have to get some eyes on it to try and resolve this. I was thinking that too. Some fresh parts may be something to try. There's a place in Brampton that stocks parts and repairs. Luckily it's not completely broken just not functioning and making leather work unfun haha. Thanks for the input!
  12. Thanks so much! That did the trick so far. I was able to move the feed dog over to clear the hook during the rotation. Now the original issues persists. I have some videos I’ll share to show. The notch in my throat plate doesn’t leave enough room for the thread to nicely pass by and form the knot. It snags and pulls leaving a bad bottom stitch. Since it is used I wonder if the throat plate is an off make and the notch isn’t normal size. I did try the lever adjustment to position the groove in Uwe’s video but thought no luck. Thanks again!
  13. Hello, Hoping to find the great sewing machine minds for some help. I have a used Juki 1341 and the hook is hitting the feed dog and needle. It seems like there is not enough space for it to turn and pass the needle. Is there an adjustment to slide the hook assembly? The main issue I had before this was that the thread was binding on the notch as it passes to form the knot. The thread would snag there, clunk and pull up. This made the tension off and knots were not formed. Thread is 207. So far I have gone through the timing sequences and needle bar height. Everything looks good there if it didn’t hit the feed dog or needle. I will get some videos but for now thought I would start with this. Thanks for the help!
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