Jump to content
weldtoride

No-weld DIY speed reducer

Recommended Posts

First of all, thanks to everyone here who posted about their own DIY speed reducers, I studied all that I could find.

A couple years back, I ran across a Singer 111W155 at a church sale, on a table complete with clutch motor.  At the sale it looked oiled and cared for; the drawer under the table contained bobbins, needles, etc.   It looked like it was just unplugged and then sat somewhere dusty for a while.  When I plugged in it ran, so I risked the $75 they were asking and brought it home.  I am trying to learn sewing for leather upholstery on a Seiko STH-8BLD-3 we already own.  However, the price on the old Singer was too tempting to pass, as I am fond of old machines.

After downloading manuals, and some fresh oil, I threaded it with #138 thread and test-sewed it.  Test sewing was extremely difficult because for me the clutch was either off, or "off to the races!"  I am familiar with TIG welding pedal controls, and still own a manual transmission truck, but the Singer clutch was beyond my patience.

Second of all, I want to thank Wiz for posts that steered me to the guys at Toledo Sewing who answered my questions about servo motors and the great service they provided me when I purchased a Consew servo motor last month. 

The Consew slowed it down tremendously, but I wanted my walking foot to crawl so I built this speed reducer.

Even though I have welding capacities,  bolting and not welding also allowed me to make changes as I went along.  My design ethic is Keep It Simple, so I came up with this.  The other part of my design ethic is use what you already have around it you can. 

I started for free in a friend's hoard of old stuff with an old set of pillow block bearings that held a 9/16" shaft that had a 2" pulley, to which I added a new 8" pulley from from Ace ($20).  

I cut two lengths of 1" square tubing to the width of my  table legs, and two squares of 3/16" steel plate big enough to mount my bearing blocks on.  

I bolted it together all with 3/8" hardware.  The two plates with the bearings sandwich the square tubing allowing it can slide front-to-aft.  The square tubing sandwiches my front and rear table legs, so It can slide up and down.  Sliding allows me to adjust the belt tensions.

I will freely admit that some of this is over-kill, but I was using what I had in my shop. If I was to buy new, I would choose 1/2" shaft and bearings, 5/16" hardware, and maybe 1/8" plate.

 

IMG_4079-L.jpg

 

Another $30 for 2 new 3L  V-belts belts and here's what I have.

 

IMG_4106-L.jpg

  

 

Edited by weldtoride
clarity

Share this post


Link to post
Share on other sites

 Well  thought out and great job, is your larger pulley 8".

Share this post


Link to post
Share on other sites

Thank you for the compliment! 

The larger pulley is an 8"  Chicago Diecast brand from Ace hardware, $20. Smaller pulley is 2" cast iron that came with the old bearings. 

Share this post


Link to post
Share on other sites
1 hour ago, weldtoride said:

The Consew slowed it down tremendously, but I wanted my walking foot to crawl so I built this speed reducer.

Nicely done. That pulley combination should knock the speed down by 75%.

kgg

Share this post


Link to post
Share on other sites

Thank you kgg,  real slow is just right for my beginner skill set.

I want to offer the original (?)  Singer motor, bracket, switchbox with capacitor, etc to anyone for pickup.  I live midway between Chicago and Milwaukee.  Lately I travel frequently to Evanston, Il, and to Ellison Bay, Wi, so could meet somewhere along way within reason.  

Serial number on sewing machine indicates 1951 production.  Motor has 2 1/2" pulley.

Moderators: Should I post in For Sale, even though it's give-way?

IMG_3958-L.jpg

 

 

  

 

Edited by weldtoride

Share this post


Link to post
Share on other sites
2 hours ago, weldtoride said:

Moderators: Should I post in For Sale, even though it's give-way?

Yes, state it is free.  Some comment about shipping or meet up.

Share this post


Link to post
Share on other sites

Nice job on the reducer, the method of adjustment is ingenious and simple.:specool:

Share this post


Link to post
Share on other sites

Join the conversation

You can post now and register later. If you have an account, sign in now to post with your account.
Note: Your post will require moderator approval before it will be visible.

Guest
Reply to this topic...

×   Pasted as rich text.   Paste as plain text instead

  Only 75 emoji are allowed.

×   Your link has been automatically embedded.   Display as a link instead

×   Your previous content has been restored.   Clear editor

×   You cannot paste images directly. Upload or insert images from URL.


×
×
  • Create New...