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What is the largest thread and needle the Pfaff 335 will sew with?

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I've used a 134-35 160 needle and 138 thread without difficulty. 

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Thanks is there and special adjustments when I change from 69 thread?

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My 335 is very fussy about #138 thread (unfortunately). First one I tried was a braided thread, the hook kept snagging the thread (I suspect it was the braid "opening up" a tiny bit as the loop was formed). Next one was Serafil, a twisted cotton/polyester blend which also snagged, but less often. Last one is a fully synthetic twisted, which still catches occasionally. I've got the hook as close as I can to the needle but it has still proven to be unreliable. I'm still working on it, as there's no reason I can see why it shouldn't work...... It's fine with #69, by the way.

I'd suggest you make sure that the hook timing is as good as you can get with the larger needle, hopefully you won't have the troubles I'm having.

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Hi Dickman If you want to pm me your address I'll send down a part roll of Strongbond for you to try if you have not already. I know it will work unless your machine is wrong. If you want more then I could arrange for them to ship to you on my acc. Regards Brian

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Just make sure the hook is set correctly for the larger needle, and both the upper and lower tensions will need some tweaking. It's never been a big deal.

Edited by Hockeymender

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On 31/07/2016 at 7:50 PM, RockyAussie said:

Hi Dickman If you want to pm me your address I'll send down a part roll of Strongbond for you to try if you have not already. I know it will work unless your machine is wrong. If you want more then I could arrange for them to ship to you on my acc. Regards Brian

Hey Dikman sent a pm with post tracking number. Regards Brian

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Brian, the thread arrived today, many thanks (but I wish you'd at least let me pay for the postage!).

I loaded up the Pfaff and ran 12" or so of stitches down an old belt - no snagging, but I did get a lot of dropped stitches!! Oh well, I figured that might be easier to deal with than the snagging. I fiddled with the tension, but that had no effect. It was fine if I went very slow, but as soon as I picked up speed it became unreliable. Something I learned a long time ago (when fault-finding telephone exchanges!) was to listen to the rhythm of machinery when it's working. So, I listened to the mechanical "rattling" of the machine as it stitched, and could soon tell when it dropped stitches by the change in sound from the bobbin area. I then noticed that the bobbin drive shaft had a little bit of back and forth play in it and traced this to the top shaft bevel gears. Unlikely to be the problem, I think, but after a bit of stuffing around I managed to take up the slack, but I'm now wondering if the bobbin case has too much play in the race assembly.

I'll have to experiment a bit more, but I'm having a rest at the moment (haven't been feeling too well for a while, gastro etc :().

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